diff options
author | Jesse Brandeburg <jesse.brandeburg@intel.com> | 2021-09-20 12:30:14 -0700 |
---|---|---|
committer | Tony Nguyen <anthony.l.nguyen@intel.com> | 2021-10-19 10:45:17 -0700 |
commit | 23be7075b31863da9cf3983aebcc8ff7537c06ac (patch) | |
tree | 239ccf6c47bf7c1df73ab43561e123f3ac249c20 /drivers/net | |
parent | d16a4f45f3a3afcb56910a7242cc621c071e80e4 (diff) | |
download | linux-23be7075b31863da9cf3983aebcc8ff7537c06ac.tar.bz2 |
ice: fix software generating extra interrupts
The driver tried to work around missing completion events that occurred
while interrupts are disabled, by triggering a software interrupt
whenever we exit polling (but we had to have polled at least once).
This was causing a *lot* of extra interrupts for some workloads like
NVMe over TCP, which resulted in regressions in performance. It was also
visible when polling didn't prevent interrupts when busy_poll was
enabled.
Fix the extra interrupts by utilizing our previously unused 3rd ITR
(interrupt throttle) index and set it to 20K interrupts per second, and
then trigger a software interrupt within that rate limit.
While here, slightly refactor the code to avoid an overwrite of a local
variable in the case of wb_en = true.
Fixes: b7306b42beaf ("ice: manage interrupts during poll exit")
Signed-off-by: Jesse Brandeburg <jesse.brandeburg@intel.com>
Tested-by: Gurucharan G <gurucharanx.g@intel.com>
Signed-off-by: Tony Nguyen <anthony.l.nguyen@intel.com>
Diffstat (limited to 'drivers/net')
-rw-r--r-- | drivers/net/ethernet/intel/ice/ice_hw_autogen.h | 1 | ||||
-rw-r--r-- | drivers/net/ethernet/intel/ice/ice_txrx.c | 26 |
2 files changed, 16 insertions, 11 deletions
diff --git a/drivers/net/ethernet/intel/ice/ice_hw_autogen.h b/drivers/net/ethernet/intel/ice/ice_hw_autogen.h index 76021d977b60..a49082485642 100644 --- a/drivers/net/ethernet/intel/ice/ice_hw_autogen.h +++ b/drivers/net/ethernet/intel/ice/ice_hw_autogen.h @@ -182,6 +182,7 @@ #define GLINT_DYN_CTL_INTERVAL_S 5 #define GLINT_DYN_CTL_INTERVAL_M ICE_M(0xFFF, 5) #define GLINT_DYN_CTL_SW_ITR_INDX_ENA_M BIT(24) +#define GLINT_DYN_CTL_SW_ITR_INDX_S 25 #define GLINT_DYN_CTL_SW_ITR_INDX_M ICE_M(0x3, 25) #define GLINT_DYN_CTL_WB_ON_ITR_M BIT(30) #define GLINT_DYN_CTL_INTENA_MSK_M BIT(31) diff --git a/drivers/net/ethernet/intel/ice/ice_txrx.c b/drivers/net/ethernet/intel/ice/ice_txrx.c index 1373b97b117a..8f908af9bdd5 100644 --- a/drivers/net/ethernet/intel/ice/ice_txrx.c +++ b/drivers/net/ethernet/intel/ice/ice_txrx.c @@ -1361,21 +1361,25 @@ static void ice_enable_interrupt(struct ice_q_vector *q_vector) if (test_bit(ICE_DOWN, vsi->state)) return; - /* When exiting WB_ON_ITR, let ITR resume its normal - * interrupts-enabled path. + /* trigger an ITR delayed software interrupt when exiting busy poll, to + * make sure to catch any pending cleanups that might have been missed + * due to interrupt state transition. If busy poll or poll isn't + * enabled, then don't update ITR, and just enable the interrupt. */ - if (wb_en) + if (!wb_en) { + itr_val = ice_buildreg_itr(ICE_ITR_NONE, 0); + } else { q_vector->wb_on_itr = false; - itr_val = ice_buildreg_itr(ICE_ITR_NONE, 0); - /* trigger an immediate software interrupt when exiting - * busy poll, to make sure to catch any pending cleanups - * that might have been missed due to interrupt state - * transition. - */ - if (wb_en) { + /* do two things here with a single write. Set up the third ITR + * index to be used for software interrupt moderation, and then + * trigger a software interrupt with a rate limit of 20K on + * software interrupts, this will help avoid high interrupt + * loads due to frequently polling and exiting polling. + */ + itr_val = ice_buildreg_itr(ICE_IDX_ITR2, ICE_ITR_20K); itr_val |= GLINT_DYN_CTL_SWINT_TRIG_M | - GLINT_DYN_CTL_SW_ITR_INDX_M | + ICE_IDX_ITR2 << GLINT_DYN_CTL_SW_ITR_INDX_S | GLINT_DYN_CTL_SW_ITR_INDX_ENA_M; } wr32(&vsi->back->hw, GLINT_DYN_CTL(q_vector->reg_idx), itr_val); |