summaryrefslogtreecommitdiffstats
path: root/sound/arm
diff options
context:
space:
mode:
Diffstat (limited to 'sound/arm')
-rw-r--r--sound/arm/pxa2xx-ac97-lib.c18
1 files changed, 17 insertions, 1 deletions
diff --git a/sound/arm/pxa2xx-ac97-lib.c b/sound/arm/pxa2xx-ac97-lib.c
index 1ecd0a66ecd3..fff7753e35c1 100644
--- a/sound/arm/pxa2xx-ac97-lib.c
+++ b/sound/arm/pxa2xx-ac97-lib.c
@@ -18,6 +18,7 @@
#include <linux/delay.h>
#include <linux/module.h>
#include <linux/io.h>
+#include <linux/gpio.h>
#include <sound/ac97_codec.h>
#include <sound/pxa2xx-lib.h>
@@ -344,8 +345,21 @@ int pxa2xx_ac97_hw_probe(struct platform_device *dev)
}
if (cpu_is_pxa27x()) {
- /* Use GPIO 113 as AC97 Reset on Bulverde */
+ /*
+ * This gpio is needed for a work-around to a bug in the ac97
+ * controller during warm reset. The direction and level is set
+ * here so that it is an output driven high when switching from
+ * AC97_nRESET alt function to generic gpio.
+ */
+ ret = gpio_request_one(reset_gpio, GPIOF_OUT_INIT_HIGH,
+ "pxa27x ac97 reset");
+ if (ret < 0) {
+ pr_err("%s: gpio_request_one() failed: %d\n",
+ __func__, ret);
+ goto err_conf;
+ }
pxa27x_assert_ac97reset(reset_gpio, 0);
+
ac97conf_clk = clk_get(&dev->dev, "AC97CONFCLK");
if (IS_ERR(ac97conf_clk)) {
ret = PTR_ERR(ac97conf_clk);
@@ -388,6 +402,8 @@ EXPORT_SYMBOL_GPL(pxa2xx_ac97_hw_probe);
void pxa2xx_ac97_hw_remove(struct platform_device *dev)
{
+ if (cpu_is_pxa27x())
+ gpio_free(reset_gpio);
GCR |= GCR_ACLINK_OFF;
free_irq(IRQ_AC97, NULL);
if (ac97conf_clk) {